Further 3D printed soft jaws for the Thwaites clock escape wheel

More use of 3D printed Soft Jaws

A few posts ago I talked about using 3D printed soft jaws for work holding in CNC operations.   This method does not replace conventional aluminium soft jaws where high accuracy machining operations are to take place.  Instead it is intended to allow second side ‘decking’ of what would have been excess stock on the material blank that had been used for work holding.

I am currently creating missing components for a Thwaites turret clock.  I had finished the pallets and I now moved onto the new escape wheel.   The design was created in Fusion 360 and integrated the pallets and the escape wheel together so the critical geometry was compatible.

The brass blank for the escape wheel was a 1/4″ brass block which I managed to hold tightly in the machine vice with a 1mm thickness of gripping stock.  (I don’t have Tallon grips or similar so I have to be generous).  I machined the wheel and was left with this 1mm to skim off the reverse side of the wheel.

I did not want the teeth on the new wheel to get damaged when gripped in the vice so the 3D printed soft jaw concept appealed.   The PLA would provide grip.   The teeth on the wheel could bite into the PLA without suffering any damage.

I had already created a single blank soft jaw In Fusion 360 for the previous pallet holding job.   This like it would be fine to accommodate the wheel dimensions.   I simply had to import two of these into the new soft jaw design (not forgetting to ‘Break the Link’ so the jaw models could be edited). I projected the wheel onto the soft jaw’s face and added a 0.2mm positive offset border.   I almost made the mistake of forgetting to invert the wheel as the soft jaw image must be a mirror of the Fusion top side view of the design to be gripped.

Fusion 360 view of the Thwaites wheel projected onto the PLA 3D printed soft jaws
Fusion 360 view of the Thwaites wheel projected onto the PLA 3D printed soft jaws.

The finished brass wheel did not accurately reflect the geometry of the Fusion design.  This is because the resolution of the tight corner CNC operations were limited to tool sizes.   I added fillets to all the ‘sharp’ edges in the soft jaw image to accommodate this.   I also had to do some tweaking of the inter jaw spacing 3D joint to reflect the wheel diameter and the amount of grip I judged might be needed.

Close up view of the fillet modifications to the sharp corners of the wheel outline
Close up view of the fillet modifications to the projected sharp corners of the wheel outline into the soft jaws.
Soft jaws and wheel ready to be skimmed
Soft jaws and the brass wheel ready to be skimmed.   The residual original square stock has been roughly trimmed around the wheel circumference.
The jaws were printed and I have to say were somewhat cosy tight around the wheel geometry.   When the jaws were mounted in the machine vice, the wheel was not going anywhere and the excess backing brass was skimmed off quickly and easily with no apparent movement of the wheel in the jaws.
Finished wheel mounted in the jaws after excess stock had been skimmed off
Finished wheel mounted in the jaws after the excess work holding stock had been skimmed off.
The finished escape wheel and pallets mounted in the Thwaites clock
The finished escape wheel and pallets mounted in the Thwaites clock

I am really warming to this technique.   It is quick and easy to implement and any mistakes can be quickly rectified with a new 3D print without having to remake aluminium versions.  I like it and recommend it.

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Vice soft jaws and then soft soft vice jaws

A Different Approach to Soft Jaws

A comment that I often make is about how having varied resources available to do a job creates on the one hand a quandary as to what route to take but on the other hand it can lead to a light bulb moment. Having a 3D printer available along side a CNC machine often creates this dilemma and often to advantage. 

Stick with me on this.

I am currently immersed in creating parts for an old turret (church) clock as pictured below.   My wife put it down as a JSN job but once again the challenge it presented won the day.  

view of the church clock as delivered to me to work on
Not a pretty sight but things do seem to move and things are certainly missing.

The client found me from my blog entry about creating the Brocot wheel in CNC.   His clock as you can see is missing the pallet arbor, pallets, crutch and arbor suspension bracket.  If that wasn’t enough it also needs a new escape wheel.  This is very similar to the aforementioned Brocot wheel but smaller in size.  Fortunately the old escape wheel was still in place but in poor shape with the teeth ends fairly battered and one tooth partially missing.

I created the CAM for the new escape wheel in Fusion 360 and then from the wheel design created the geometry for the pallets.  (There is a great document created by the BHI as part of their DLC called ‘Drawing Clock and Watch Escapements’ that helped on this as did W.J. Gazeley’s book ‘Clock and Watch Escapements’). In order to check the pallet design I decided to first of all print a 3D model.   The printed part looked like it would work when tried against the original battered escape wheel.

Next step in my evolutionary process was to make an aluminium version on the Tormach CNC.   I used a superglue mounting block and cut the pallet profile for the full 10mm stock depth and down to the blue mounting masking tape.   Because the aluminium was so soft and I kept the DOC gentle this turned out well.

Although the aluminium version worked very well and helped me prove the working of the clock,  aluminium is too soft for clock pallets.   A steel set would now needed and I opted for 20mm ground flat stock as the ideal material.  

Side #1 was cut while being held in the machine vice on parallels.  A 2mm thickness of stock was left as the gripping layer.   All went to plan.

running side 1 of the clock pallets designed in fusion 360 and running on the Tormach 440 CNC mill
Side one machining of the clock pallet. An 8mm 3D Adaptive has completed and a 4mm follow on is now being run to clean up the finish.  Note the newly installed second Fogbuster nozzle.
Side one of the clock pallets completed showing the residual stock to leave as a side two operation
Finished side 1 operations and ready to invert to remove the residual stock used to grip in the vice jaws

Side #2 now became the headache.   I could have used the super glue bonding of the stock as per the aluminium version. My twitch was that this would leave very little of the pallet material remaining to act as a secure bonding face with the superglue.  Given I was cutting steel there was every chance of things parting company.  I could hold the model inverted in the vice but there was a real danger of the nib tips getting crushed.   Not a good idea.

Clearly the right solution was to make a pair of soft jaws to grip the pallet shape while I was decking off the side #2 residual 2mm.

Now here is the light bulb moment.   I designed the soft jaws in Fusion so they would swap out the existing steel jaws on my machine vice.   This is a straightforward process using the Project function.   The best demo of this that I have seen is by Cough42 and is worth a watch.

pictorial view of the pallet soft jaws to allow side #2 material to be removed
The jazzed up Fusion view of the soft jaws (red and green) and the finished pallet shape that gets gripped in them.

I was about to order some aluminium stock to make the soft jaws when the 3D printer winked at me from the corner of the workshop.  Could I print the soft jaws on the printer and get enough grip to allow the last 2mm to be decked off ?  This had to be worth a try and had the advantage that I could be getting on with another of the clock components while they were printing.

Taking this route I decided I would need to modify the design in Fusion.   The 3D printer always leaves cavities a bit under size.  I used Fusion’s Offset Faces to increase the profile shape by 0.2mm all around.  I set the gap between the two jaws at 1mm.

Print time was around 2.5 hours for each each jaw.   With CAM and setup time, running them in aluminium would have been similar.   I gained the 5 hours to do something else.  (i.e. Drink tea watching the mill ….)

The idea worked.   The PLA tightly gripped the inverted Side #1 profile while I decked off the 2mm residual stock.  I didn’t go too aggressive on DOC.

finished pallets with PLA soft jaws
View of the finished pallets with the PLA soft jaws in the background mounted in the machine vice

 A set of PLA soft jaws – not a radical idea but food for thought.   

Aluminium soft jaws are essential if you are going to be undertaking detailed feature machining of Side #2 but if it is a simple decking skim then PLA would seem more than adequate.  Soft jaws are 1 off items dedicated to a particular part.   They are consumable as is the PLA but the PLA versions are overall quicker to produce.

This has been another situation where what would have been a no brainer ‘this is how we normally do this’ turned into a ‘how else could I do this with the resources at my disposal and make life easier ? ‘.  It is that lazy side of me shining through yet again …..   

Onwards to the next phase of the clock activity.

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CNC Work Reference Centring using Mushrooms

This is probably not original but worth commenting on.   I have a tooling plate on the bed of my Tormach PCNC440.  This has a matrix of M8 holes on 25mm spacing together with intermediate 3.7mm tooling pin holes.

Quite often I have a need to set up my work CNC coordinate system (WCS) such that it is centred on one of the M8 holes. 

If I want to do a quick and dirty centre on one of these holes then I use the Laser Centring tool as mentioned elsewhere on my blog.

If I need to be a bit more precise then I have a mushroom/top hat shaped disc with shank that is a tight fit in the tapped M8 holes.  PathPilot has a number of probing routines and these include finding the centre of a circular object.    Simply push the top hat into the desired hole and then probe the disc for centre.  You can use an active probe such as the Hallmark ITTP.

If you haven’t got an active probe you can use a Haimer.   Simply align the Haimer tip somewhere close to a maximum point on the disc circumference and advance the axis to show a reading on the Haimer.  Rock the opposite axis back and forth and watch the Haimer reading to find the high point on the circumference.   Zero the axis.   Go to the opposite side of the disc and repeat this process and divide the measured diameter by 2 for the disc centre.   Repeat on the opposite axis.

(You can use this Haimer rocking back and forth method to find the diameter high point when cross drilling a circular item to fit grub screws etc).

Hole centring mushrooms
Two examples from my ‘mushroom farm’

The mushrooms are made with a silver steel shank that is skimmed to be a non wobble (how technical is that ..) fit in M8 (~6.8mm) and an aluminium top hat that is superglued in place on the shank.   Once the glue has set the top hat is squared up while held in a collet in the lathe.  This ensures concentricity with the shank.   The disc will now sit flat to the tooling table when the shank is pressed home and perpendicular in the hole.

Clearly the larger the disc diameter the less centring error there will be.

I now have a ‘mushroom farm’ of discs for all manner of hole sizes.  It’s not rocket science but as you well know, I am all for a simple (aka lazy) approach.  Apologies to all the Grannies out there.

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Burgess BK3 Bandsaw Disaster and Repair

Some pieces of workshop equipment generate a sentimental attraction that is hard to break.  One such piece of kit is my Burgess BK3 bandsaw which is ancient but has up to now worked reasonably well for my needs.   I bought it on EBay from an owner in Lancashire and remember a nice day trip to collect it.

It is a very useful machine and gets pressed into use day in and day out.   That is until the other day when the blade came off with a loud twang.  On inspection the drive wheel had lost part of its blade outer retaining flange.   It appeared to be very old brittle plastic and the damage was really to be expected given the vintage of the device.

After head scratching I designed a replacement edging strip in Fusion 360 which I 3D printed and glued in place.   Fingers crossed that will give the machine a reprieve and extend its life.

In the course of looking for possible spares (no chance) I came across a reference to modifications to the BK3 in Model Engineer to improve the blade tracking and speed settings. Here is a link to the articles  burgessbandsaw2.  I am indebted to the members of my local model engineering club who came up trumps with copies of these articles for me.

The guide modification consisted of replacing the two stud guides with ball bearings.  While the machine was in pieces it seemed like a good idea to implement this modification.  The Fusion 360 3D model is shown below. The blade is sandwiched between the two ball races and these can be slid in and out and then be fixed in place with the cap head screws once the correct location is found to guide the blade.

I drew the replacement guide block assembly in Fusion 360 and milled it on the Tormach CNC from brass.   The 1/2″ bearings came from BearingBoys.

All is now re-assembled and running really smoothly.  The blade prefers to run in straight lines which is a revelation.

Update :  Since this blog entry I have made other modifications to my BK3 and these are contained in this link BK3 Modifications v2.

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Workshop resources all coming together like clockwork

Another JSN Job ?

You know how I keep on going on about how solutions to problems are often solved by coming at them from different and often unconventional directions, by utilising and marrying available resources ? It was a philosophy that I encouraged in my team while running my business and it has carried over into my way of working in retirement.   A recent job brought his home to me.

A client had a very old clock that had had a new barrel wheel made and fitted but the clock would not run for more than a few minutes.   There appeared to be an incompatibility either between the modulus of the new wheel and its mating pinion or the shape of the original pinion did not match the shape of the new wheel. 

If you spun the barrel wheel you could feel the resistance build up as the synchronisation between the two profiles drifted out.   Adding extra weight to the barrel helped but did not solve the problem.

So what to do ?   

The barrel wheel was serious engineering and I did not fancy making a new one.   The existing mating pinion was a seven leaf format and its leaves were what you might call pear drop shaped rather than the expected profile.  The pinion arbor had a 72 tooth wheel driving the next part of the clock train but we did have a spare one of these to hand from the minute dial.

Calculations from the geometry of the barrel wheel resulted in a modulus        figure of 1.86.  A rather large value and not one that conventional cutters are readily available for.  The pinion was perhaps something that could be drawn in Fusion 360 and then made on my Tormach CNC PCNC440 milling machine.   The only snag was that the profile needed on the pinion would likely be weird and the world’s supply of brass could diminish rapidly while getting the profile correct.

Using Gearwheel Designer I created what would be the expected profile for a 7 leaf pinion with a modulus of 1.86.  This was exported as a DXF line drawing into Fusion 360.  This outline was extruded in Fusion into a 3D design and a boss was added to mount the 72 tooth wheel. 

The design was 3D printed on my Sindoh 3DWOX printer and was mounted on a 6mm silver steel arbor.   I added a driving disc that interlocked with the printed pinion and the crossings on the wheel to drive the assembly.  Surprise surprise it didn’t run but it did mirror the regular pattern of stiffness of the original pinion. 

Original arbor , pinion and wheel with the driving disc and a test profile
The original arbor, pinion and wheel together with the driving disc and a 3D printed pinion test profile. The driving disc has screws to lock it to the wheel and two protruding pins to lock into the 3D printed pinion profile under test. The 3D printed profile was a tight pressure fit onto the new 6mm arbor.

I now had the test bed for quickly making and testing different pinion profiles. There followed a number of hours watching the engagement progression of the profile of the pinion into the barrel wheel and then trying to conceive a profile for the pinion that might run. 

3D printed test profiles
Various trial profiles and the temporary driving disc to engage with the 72 tooth wheel

 

Test pinion in place on the new arbor
A test pinion in place showing the 72 tooth wheel and the driving disc

Fusion 360 made this process so easy and round 10 printed test profiles later I had success with a clock that now ran.    The driving weight on the barrel was around 11kg and it looked to be worthwhile wasting some brass making a ‘proper’ one. 

I took the 3D design and produced CAM code in Fusion.   This would cut the profile ‘on end’ using an adaptive first cut with a 4mm end mill followed by rest machining the remaining material with a 2mm end mill. 

Images of the Fusion 360 process of creating the new 7 leaf pinion
The Fusion 3D model of the pinion, the CAM simulation of the leaf cutting, first adaptive cut of the leaves and rest machining final pinion

The resulting brass pinion was mounted on the arbor and the clock ran with a strong beat.   As expected the brass pinion gave less surface to surface resistance than the 3D printed part and the barrel driving weight was now able to be reduced down to 6.25kg.

new pinion mounted in the clock
The finished pinion mounted in the clock on the new arbor

I ran my Microset Timer on the clock overnight and had a first off timing error of 5 minutes per day which was fixable with a pendulum tweak. The movement had an instability of a few seconds per day which was quite astonishing.

The conclusion of the experience is that at first glance this seemed like a conventional pinion cutting exercise …. but M1.86 cutters are not readily available.   If a cutter could have been found at less than a King’s Ransom it is likely that the resulting conventional profile would have been wrong to match the barrel wheel.   

The alternative route that was taken of Gearwheel Designer to Fusion to 3D print to Fusion CAM to CNC machining solved the problem albeit with a final weird profile.    The purists and traditionalists will groan.   There will be a gnashing of teeth and a pulling out of hair. 

Does it really matter if the result is new life for what could have become a heap of scrap metal ?

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