Further 3D printed soft jaws for the Thwaites clock escape wheel

More use of 3D printed Soft Jaws

A few posts ago I talked about using 3D printed soft jaws for work holding in CNC operations.   This method does not replace conventional aluminium soft jaws where high accuracy machining operations are to take place.  Instead it is intended to allow second side ‘decking’ of what would have been excess stock on the material blank that had been used for work holding.

I am currently creating missing components for a Thwaites turret clock.  I had finished the pallets and I now moved onto the new escape wheel.   The design was created in Fusion 360 and integrated the pallets and the escape wheel together so the critical geometry was compatible.

The brass blank for the escape wheel was a 1/4″ brass block which I managed to hold tightly in the machine vice with a 1mm thickness of gripping stock.  (I don’t have Tallon grips or similar so I have to be generous).  I machined the wheel and was left with this 1mm to skim off the reverse side of the wheel.

I did not want the teeth on the new wheel to get damaged when gripped in the vice so the 3D printed soft jaw concept appealed.   The PLA would provide grip.   The teeth on the wheel could bite into the PLA without suffering any damage.

I had already created a single blank soft jaw In Fusion 360 for the previous pallet holding job.   This like it would be fine to accommodate the wheel dimensions.   I simply had to import two of these into the new soft jaw design (not forgetting to ‘Break the Link’ so the jaw models could be edited). I projected the wheel onto the soft jaw’s face and added a 0.2mm positive offset border.   I almost made the mistake of forgetting to invert the wheel as the soft jaw image must be a mirror of the Fusion top side view of the design to be gripped.

Fusion 360 view of the Thwaites wheel projected onto the PLA 3D printed soft jaws
Fusion 360 view of the Thwaites wheel projected onto the PLA 3D printed soft jaws.

The finished brass wheel did not accurately reflect the geometry of the Fusion design.  This is because the resolution of the tight corner CNC operations were limited to tool sizes.   I added fillets to all the ‘sharp’ edges in the soft jaw image to accommodate this.   I also had to do some tweaking of the inter jaw spacing 3D joint to reflect the wheel diameter and the amount of grip I judged might be needed.

Close up view of the fillet modifications to the sharp corners of the wheel outline
Close up view of the fillet modifications to the projected sharp corners of the wheel outline into the soft jaws.
Soft jaws and wheel ready to be skimmed
Soft jaws and the brass wheel ready to be skimmed.   The residual original square stock has been roughly trimmed around the wheel circumference.
The jaws were printed and I have to say were somewhat cosy tight around the wheel geometry.   When the jaws were mounted in the machine vice, the wheel was not going anywhere and the excess backing brass was skimmed off quickly and easily with no apparent movement of the wheel in the jaws.
Finished wheel mounted in the jaws after excess stock had been skimmed off
Finished wheel mounted in the jaws after the excess work holding stock had been skimmed off.
The finished escape wheel and pallets mounted in the Thwaites clock
The finished escape wheel and pallets mounted in the Thwaites clock

I am really warming to this technique.   It is quick and easy to implement and any mistakes can be quickly rectified with a new 3D print without having to remake aluminium versions.  I like it and recommend it.

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Vice soft jaws and then soft soft vice jaws

A Different Approach to Soft Jaws

A comment that I often make is about how having varied resources available to do a job creates on the one hand a quandary as to what route to take but on the other hand it can lead to a light bulb moment. Having a 3D printer available along side a CNC machine often creates this dilemma and often to advantage. 

Stick with me on this.

I am currently immersed in creating parts for an old turret (church) clock as pictured below.   My wife put it down as a JSN job but once again the challenge it presented won the day.  

view of the church clock as delivered to me to work on
Not a pretty sight but things do seem to move and things are certainly missing.

The client found me from my blog entry about creating the Brocot wheel in CNC.   His clock as you can see is missing the pallet arbor, pallets, crutch and arbor suspension bracket.  If that wasn’t enough it also needs a new escape wheel.  This is very similar to the aforementioned Brocot wheel but smaller in size.  Fortunately the old escape wheel was still in place but in poor shape with the teeth ends fairly battered and one tooth partially missing.

I created the CAM for the new escape wheel in Fusion 360 and then from the wheel design created the geometry for the pallets.  (There is a great document created by the BHI as part of their DLC called ‘Drawing Clock and Watch Escapements’ that helped on this as did W.J. Gazeley’s book ‘Clock and Watch Escapements’). In order to check the pallet design I decided to first of all print a 3D model.   The printed part looked like it would work when tried against the original battered escape wheel.

Next step in my evolutionary process was to make an aluminium version on the Tormach CNC.   I used a superglue mounting block and cut the pallet profile for the full 10mm stock depth and down to the blue mounting masking tape.   Because the aluminium was so soft and I kept the DOC gentle this turned out well.

Although the aluminium version worked very well and helped me prove the working of the clock,  aluminium is too soft for clock pallets.   A steel set would now needed and I opted for 20mm ground flat stock as the ideal material.  

Side #1 was cut while being held in the machine vice on parallels.  A 2mm thickness of stock was left as the gripping layer.   All went to plan.

running side 1 of the clock pallets designed in fusion 360 and running on the Tormach 440 CNC mill
Side one machining of the clock pallet. An 8mm 3D Adaptive has completed and a 4mm follow on is now being run to clean up the finish.  Note the newly installed second Fogbuster nozzle.
Side one of the clock pallets completed showing the residual stock to leave as a side two operation
Finished side 1 operations and ready to invert to remove the residual stock used to grip in the vice jaws

Side #2 now became the headache.   I could have used the super glue bonding of the stock as per the aluminium version. My twitch was that this would leave very little of the pallet material remaining to act as a secure bonding face with the superglue.  Given I was cutting steel there was every chance of things parting company.  I could hold the model inverted in the vice but there was a real danger of the nib tips getting crushed.   Not a good idea.

Clearly the right solution was to make a pair of soft jaws to grip the pallet shape while I was decking off the side #2 residual 2mm.

Now here is the light bulb moment.   I designed the soft jaws in Fusion so they would swap out the existing steel jaws on my machine vice.   This is a straightforward process using the Project function.   The best demo of this that I have seen is by Cough42 and is worth a watch.

pictorial view of the pallet soft jaws to allow side #2 material to be removed
The jazzed up Fusion view of the soft jaws (red and green) and the finished pallet shape that gets gripped in them.

I was about to order some aluminium stock to make the soft jaws when the 3D printer winked at me from the corner of the workshop.  Could I print the soft jaws on the printer and get enough grip to allow the last 2mm to be decked off ?  This had to be worth a try and had the advantage that I could be getting on with another of the clock components while they were printing.

Taking this route I decided I would need to modify the design in Fusion.   The 3D printer always leaves cavities a bit under size.  I used Fusion’s Offset Faces to increase the profile shape by 0.2mm all around.  I set the gap between the two jaws at 1mm.

Print time was around 2.5 hours for each each jaw.   With CAM and setup time, running them in aluminium would have been similar.   I gained the 5 hours to do something else.  (i.e. Drink tea watching the mill ….)

The idea worked.   The PLA tightly gripped the inverted Side #1 profile while I decked off the 2mm residual stock.  I didn’t go too aggressive on DOC.

finished pallets with PLA soft jaws
View of the finished pallets with the PLA soft jaws in the background mounted in the machine vice

 A set of PLA soft jaws – not a radical idea but food for thought.   

Aluminium soft jaws are essential if you are going to be undertaking detailed feature machining of Side #2 but if it is a simple decking skim then PLA would seem more than adequate.  Soft jaws are 1 off items dedicated to a particular part.   They are consumable as is the PLA but the PLA versions are overall quicker to produce.

This has been another situation where what would have been a no brainer ‘this is how we normally do this’ turned into a ‘how else could I do this with the resources at my disposal and make life easier ? ‘.  It is that lazy side of me shining through yet again …..   

Onwards to the next phase of the clock activity.

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Workshop resources all coming together like clockwork

Another JSN Job ?

You know how I keep on going on about how solutions to problems are often solved by coming at them from different and often unconventional directions, by utilising and marrying available resources ? It was a philosophy that I encouraged in my team while running my business and it has carried over into my way of working in retirement.   A recent job brought his home to me.

A client had a very old clock that had had a new barrel wheel made and fitted but the clock would not run for more than a few minutes.   There appeared to be an incompatibility either between the modulus of the new wheel and its mating pinion or the shape of the original pinion did not match the shape of the new wheel. 

If you spun the barrel wheel you could feel the resistance build up as the synchronisation between the two profiles drifted out.   Adding extra weight to the barrel helped but did not solve the problem.

So what to do ?   

The barrel wheel was serious engineering and I did not fancy making a new one.   The existing mating pinion was a seven leaf format and its leaves were what you might call pear drop shaped rather than the expected profile.  The pinion arbor had a 72 tooth wheel driving the next part of the clock train but we did have a spare one of these to hand from the minute dial.

Calculations from the geometry of the barrel wheel resulted in a modulus        figure of 1.86.  A rather large value and not one that conventional cutters are readily available for.  The pinion was perhaps something that could be drawn in Fusion 360 and then made on my Tormach CNC PCNC440 milling machine.   The only snag was that the profile needed on the pinion would likely be weird and the world’s supply of brass could diminish rapidly while getting the profile correct.

Using Gearwheel Designer I created what would be the expected profile for a 7 leaf pinion with a modulus of 1.86.  This was exported as a DXF line drawing into Fusion 360.  This outline was extruded in Fusion into a 3D design and a boss was added to mount the 72 tooth wheel. 

The design was 3D printed on my Sindoh 3DWOX printer and was mounted on a 6mm silver steel arbor.   I added a driving disc that interlocked with the printed pinion and the crossings on the wheel to drive the assembly.  Surprise surprise it didn’t run but it did mirror the regular pattern of stiffness of the original pinion. 

Original arbor , pinion and wheel with the driving disc and a test profile
The original arbor, pinion and wheel together with the driving disc and a 3D printed pinion test profile. The driving disc has screws to lock it to the wheel and two protruding pins to lock into the 3D printed pinion profile under test. The 3D printed profile was a tight pressure fit onto the new 6mm arbor.

I now had the test bed for quickly making and testing different pinion profiles. There followed a number of hours watching the engagement progression of the profile of the pinion into the barrel wheel and then trying to conceive a profile for the pinion that might run. 

3D printed test profiles
Various trial profiles and the temporary driving disc to engage with the 72 tooth wheel

 

Test pinion in place on the new arbor
A test pinion in place showing the 72 tooth wheel and the driving disc

Fusion 360 made this process so easy and round 10 printed test profiles later I had success with a clock that now ran.    The driving weight on the barrel was around 11kg and it looked to be worthwhile wasting some brass making a ‘proper’ one. 

I took the 3D design and produced CAM code in Fusion.   This would cut the profile ‘on end’ using an adaptive first cut with a 4mm end mill followed by rest machining the remaining material with a 2mm end mill. 

Images of the Fusion 360 process of creating the new 7 leaf pinion
The Fusion 3D model of the pinion, the CAM simulation of the leaf cutting, first adaptive cut of the leaves and rest machining final pinion

The resulting brass pinion was mounted on the arbor and the clock ran with a strong beat.   As expected the brass pinion gave less surface to surface resistance than the 3D printed part and the barrel driving weight was now able to be reduced down to 6.25kg.

new pinion mounted in the clock
The finished pinion mounted in the clock on the new arbor

I ran my Microset Timer on the clock overnight and had a first off timing error of 5 minutes per day which was fixable with a pendulum tweak. The movement had an instability of a few seconds per day which was quite astonishing.

The conclusion of the experience is that at first glance this seemed like a conventional pinion cutting exercise …. but M1.86 cutters are not readily available.   If a cutter could have been found at less than a King’s Ransom it is likely that the resulting conventional profile would have been wrong to match the barrel wheel.   

The alternative route that was taken of Gearwheel Designer to Fusion to 3D print to Fusion CAM to CNC machining solved the problem albeit with a final weird profile.    The purists and traditionalists will groan.   There will be a gnashing of teeth and a pulling out of hair. 

Does it really matter if the result is new life for what could have become a heap of scrap metal ?

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Making a Brocot Escape Wheel using Fusion 360 and Tormach PCNC440 CNC milling machine

A Steep Learning Curve

My wife has presented me with a sign that has just got JSN written on it.  It is to remind me when I answer the phone to a ‘can you just do’ enquiry…… to Just Say No.

I try my best to live up to her expectations but sometimes something comes along that should really be a JSN job but which scratches an itch.   You know what I mean.   You think about it and you do all the right mental arithmetic in your head and the answer keeps coming back to the same – don’t even think about it.  But the the other side of my brain is screaming at me … what a challenge, what a learning experience, what fun to have a go at it.   Providing the asking party is aware of your thought process or lack of it and accepts that it might just go belly up and never come to fruition then why not ?

Back to the story – 10 days or so ago I had a call from David Pawley who is a turret clock expert extraordinaire to say someone he knew was after an escape wheel for a turret clock and was desperate.   David passed on the details and a couple of days later the potential customer arrived on our driveway.  After a suitably socially distant conversation and a rubber gloves inspection of the old damaged wheel …. I got sucked in and turned the JSN sign over to face the wall.

Brocot 30 tooth escape wheel
The original Brocot 30 tooth escape wheel that needed a new one making

As you can see it is not an ordinary escape wheel and I had to delve into one of my favourite books ‘Wheel and Pinion Cutting in Horology’ by J Malcolm Wild FBHI in order to learn about Brocot Escape wheels.   Malcolm is a great guy and his book should be on any clock experimenters bookcase.

The Brocot is no ordinary escape wheel.   In fact it is a real challenge.   Not a simple fly cutter job.  Traditionally it would be cut in an indexing device such as a lathe with two different cutters, one for the curve and one for the notch.  I didn’t have these so I thought I would probably upset the traditionalists and try to use CNC.

Read all about the adventure and see the result in this pdf download …….

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Silencing the Bill Smith Gearless Gravity Arm Clock

You will find details of my activity building the Bill Smith Hip Toggle Gearless Gravity Arm clock elsewhere on my site.   This was the first clock I ever made and it taught me a lot about techniques all of which were well documented by Bill in his write up and in his many other books and videos.

Let me state now that the clock design as intended by Bill works and works well.  It has one distinct disadvantage that every minute or so it gives a very loud ‘clunk’ as the pendulum amplitude diminishes, the hip toggle triggers and the solenoid resets.    Running it in the workshop was fine as I became immune to the noise but sadly the clock will never progress into the house given my wife’s sensitivity to noise.

This has been a frustration to me as the clock looks splendid and its motion work action is a fascination to behold.  It deserves to be on display in a more public arena than the workshop.

All of which lead to some head scratching and a compromise re-design.   If I accept that the clock is an electro-mechanical device then my conscience allows me to consider other electro-mechanical solutions that are significantly less noisy.   This is the fundamental premise to my re-design.

There are many clock designs that use magnetism attraction and repulsion as the driving force and my thoughts turned to this as a potential solution.

I 3D printed a magnet holder to fit on the pendulum rod.   This holds two magnets.   There is a large one facing the direction of swing and a small one perpendicular to the swing towards the backboard.  I mounted a Hall Effect Sensor (HES) on a prototype board onto the back board at the mid swing position.   The gist of my idea was to have the pendulum swinging back and forth across the HES with the HES being triggered by the small magnet.   I would count the number of swings detected by the HES and after a defined number of swings I would energize a solenoid to repel the large magnet.

There was a little bit of electronics involved.   I had a 4060 binary counter counting the swings and used the divide by 32 output to trigger a 555 in monostable mode.   This would create a delay period from the mid point to the end of swing before the solenoid was energized.   A second 555 would then define how long the solenoid repelling pulse would last.   I also added LED indicators to all key timing points so I can easy diagnose what was going on.   I also allowed selection of the 16,32 and 64 divisions from the 4060 until I established the optimum choice.

The pendulum period is 4800 beats per minute so one swing lasts for 750ms.  The first 555 must therefore provide a delay of 375ms before energizing the solenoid.   The second 555 delay would be a ‘suck it and see’ period to be determined.

The concept was lashed up and worked OK …. except that the pendulum amplitude just grew and grew until the large pendulum magnet attached itself to the solenoid core …. not a good idea .   What was needed was a maximum amplitude detector to act as feedback to inhibit the solenoid pulse action.   

A second HES was mounted at a position that represented the maximum swing position and the output from this, when triggered, would feed back to the 4060 RESET pin to stop the count until the amplitude diminished sufficiently.   This worked and the result was very repeatable.   There was one proviso that the pendulum must be started by triggering the over swing HES and releasing.   Without this the 4060 could be one count out of step and would energize the solenoid as the pendulum was swinging back from its furthest point.  This would cause a repelling and slowing of the swing.

Overview image of the new pendulum sustaining mechanism on the Bill Smith Gearless Gravity Arm clock
Overview image of the new pendulum sustaining mechanism. Top left is the timing board and lower right is the Hall Effect Sensor board. The solenoid is the original Bill Smith design. The white block on the pendulum is the magnets holder. You can see the two Hall Effect Sensors hanging below the blue prototyping board.
close up view of the sensor board
A close up view of the Hall Effect Sensor board where the two sensors can be more clearly seen along with diagnostic LEDs and interface converters to the timing board.  The pendulum magnet holder can just be seen coming into shot.
Oscilloscope display of the new timing sequence for the Bill Smith Gearless clock
Oscilloscope display showing the yellow regular negative going pulse from the centre swing HES detector, the blue delay pulse to allow the pendulum to travel to its extreme and commence its swing back and the purple pulse triggered from the back edge of the delay pulse which defines the solenoid ‘On’ time.

The prototype has proved the concept but I now need to engineer a clean solution.   First choice is perhaps an Arduino Mini but it could also be PIC based.   

More to follow.

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